WoS İndeksli Yayınlar Koleksiyonu
Permanent URI for this collectionhttps://hdl.handle.net/20.500.12573/394
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Article Citation - WoS: 25Citation - Scopus: 28Passive Flow Control Application Using Single and Double Vortex Generator on S809 Wind Turbine Airfoil(MDPI, 2023-07-12) Ozden, Mustafa; Genc, Mustafa Serdar; Koca, KemalThe current study is aimed at investigating the influences of vortex generator (VG) applications mounted to the suction and pressure surfaces of the S809 wind turbine airfoil at low Reynolds number flow conditions. Both single and double VG applications were investigated to provide technological advancement in wind turbine blades by optimizing their exact positions on the surface of the airfoil. The results of the smoke-wire experiment for the uncontrolled case reveal that a laminar separation bubble formed near the trailing edge of the suction surface, and it was moved towards the leading edge as expected when the angle of attack was increased, resulting in bubble burst and leading-edge flow separation at & alpha; = 12 & DEG;. The u/U-& INFIN;, laminar kinetic energy and total fluctuation energy contours obtained from the numerical study clearly show that both the single and double VG applications produced small eddies, and those eddies in the double VG case led the flow to be reattached at the trailing edge of the suction surface and to gain more momentum by energizing. This situation was clearly supported by the results of aerodynamic force; the double VG application caused the lift coefficient to increase, resulting in an enhancement of the aerodynamic performance. A novel finding is that the VG at the pressure surface caused the flow at the wake region to gain more energy and momentum, resulting in a reattached and steadier flow condition.Article Citation - WoS: 1Citation - Scopus: 1Measurements of Flow Characterization Revealing Transition to Turbulence Associated With the Partial Flexibility-Based Flow Control at Low Reynolds Number(Springer Heidelberg, 2024-07-26) Koca, Kemal; Keskin, Sinem; Sahin, Rumeysa; Veerasamy, Dhamotharan; Genc, Mustafa SerdarIn order to comprehend the flow characteristics of both controlled and uncontrolled SD7062 wind turbine airfoils with local flexible membrane material throughout a variety of angles of attack at a Reynolds number of 1.05 x 105, an experimental investigation was conducted. The time-dependent force measurement, the hot-wire experiment with a boundary layer and glue-on probes, and the oil-flow visualization technique were all utilized in the present study to measure the flow over the airfoil and examine the laminar-turbulent transition, laminar separation bubble, and the impact of a special flow control method that uses flexibility. A comprehensive intermittency analysis by utilizing hot-wire results was employed to obtain the flow physics effects of the local flexibility the first in the literature. The key results of the experiment demonstrated that the stall was delayed from alpha = 10 degrees to 12 degrees by the local flexibility. The hot-wire results are dedicated to laminar, transitional and turbulent regions and the transition phenomena at different locations over the suction surface of the airfoil in the analysis graphs. As demonstrated by the results of the oil-flow visualization experiment, in the uncontrolled case, the laminar separation bubble formed over the airfoil at alpha = 8 degrees between x/c = 0.16 and x/c = 0.42. The use of flexible membrane material over the airfoil provided that the oscillation of this material triggered the transition to turbulence and a bypass transition, which resulted in the reattached flow.
